AJ installed the zincs.
We installed two LED lights on the hull
under the cockpit. Underwater marine lights run into the low
hundreds, but the Chinese make 750 lumens waterproof cast acrylic LEDs for $15,
complete with rubber pads. So we gifted ourselves and installed
something fun. We'll be able to light up clear tropical waters under
the boat and attract the creatures. Also, they could be quite useful
for servicing the prop or rudder under water. They install with 4
skinny screws, and a hole for the wires to enter the boat. I sanded
off the bottom paint where they would be placed. We caulked both
sides of the rubber backing pad, gluing the light to the pad and the
pad to the hull. Then AJ screwed it through the hull into the cockpit
lockers.
The bilge pump was installed. We have a
second one to place above this one, but it's missing it's screen. So
we'll add that one once we get that replaced. That portion of the
bilge will get painted with the rest of the subfloors eventually.
I painted the gudgeon and prop, then
taped off the waterline for a touch up. I still had almost 2/3 a
gallon of paint left after that, so I gave the rest of the bottom one
last coat. It's been 6 months or more since it was painted, so it was
in need of reactivation anyway. I'm glad we had just barely enough
left over to cover it!
We installed most of the deck hardware
before we left for Christmas. The two aft cleats, vents, dorades, etc.. We are
using starboard pads instead of wood this time. No varnish, no rot.
Easy peasy. I liked how it turned out, the white pads make the deck
look a lot less cluttered. We caulked the deck hardware with 4000
UV, and through bolted.
You may have noticed that there is only one cleat up front. We intended to remove and re-bed both, but the one shown refused to come off. It leaks into the anchor locker, but it's solid. We would have installed the other one, but we could not find the right size bolts in town. Except for at West Marine, who wanted $5.00 per bolt. We only need 8 for both cleats, but we just couldn't suck up the cost when we can order all 8 for $5.00 online. Even with overnight shipping we'd save $25.00. So we decided to launch with just the one. It will hold until the bolts arrive regular mail, and we can install the second one. The stubborn one is on wood pads, but Danny painted over them. They're awl-gripped in, thus match the starboard pads of the second one.. Maybe we should smear some caulk on the bolts and let it be.
You may have noticed that there is only one cleat up front. We intended to remove and re-bed both, but the one shown refused to come off. It leaks into the anchor locker, but it's solid. We would have installed the other one, but we could not find the right size bolts in town. Except for at West Marine, who wanted $5.00 per bolt. We only need 8 for both cleats, but we just couldn't suck up the cost when we can order all 8 for $5.00 online. Even with overnight shipping we'd save $25.00. So we decided to launch with just the one. It will hold until the bolts arrive regular mail, and we can install the second one. The stubborn one is on wood pads, but Danny painted over them. They're awl-gripped in, thus match the starboard pads of the second one.. Maybe we should smear some caulk on the bolts and let it be.
Monday night Robin was slung in preparation for a Tuesday morning splash at high tide.
The lead keel dented from the front
stand! Maybe we were on the hard too long...
We arrived at 7 am on Tuesday for a 7:30 high tide splash.
Docking went off without a hitch. Though it took some lassoing skills to catch the aft pilings.
So far so good. So far so excellent
actually after we discovered this:
We installed the pulpit and 3 stanchions on the hard before launch. When we were cleaning the pulpit bases we found the hull number etched into the bottom. It's the original Hong Kong stainless pulpit, and is still in great shape. It was dingy and rusty after sitting under the boat so long. Surprisingly, the surface rust came right off with Comet stainless appliance cleaner and a Brillo pad. We gave it a little polish after that.
We installed the rest of the stanchions
after we docked. All except for the two gates. We still have to
make a couple pads for them. I
caulked and dropped the bolts in from the outside and AJ cranked down
the nuts and washers on the inside.
It's looking more like a boat every
day!
P.S. My hard drive with all our travel pictures, music and movies died. My entire digital media collection is gone forever. But there's more bad news, half of the pictures on this blog have vanished also. I have to re-upload them all, only I don't have all of them anymore, so I must spend hours reclaiming them from Flickr. But the good news is there is wifi at the dock! Which means I can blog! And start rebuilding my media collection.. and start replacing the pics on the old posts. *sigh*
CONGRATS. guys!
ReplyDeleteand the boat looks great afloat.
AJ, whenever you might get a chance, it would be great to get some feedback on the new tiller> remember, I also have a Luders 36 and I would like to get rid of the wheel and the associated cables and complications.
am wondering if the new hardware is solid enough and how the tiller to the rudderstock connection works> if so, any chance of getting the specs on what you had made up?
looking forward to your next post> db//
Sorry about the forever delay. I could gladly talk all day on that tiller head! In fact it might even be easier over email or the phone!
DeleteLet me summarize first: After Tillerhead 1.0, I asked an engineer to help us in this area. He was a friend, and did it kindly in his spare time, but his knowledge of material properties and strength calculations were critical to Version 2.0, which still hasn't been finished nor tested.
After toying around a bit with some numbers and a LITTLE of my own experience with the steering effort generated by the tiller version 1.0, I would estimate the boat is capable of generating nearly 100 pounds of force on the end of my tiller in the absolute worst conditions. That isn't easy to hold on to, but I assume we want a tiller anyway, mainly because of all the reasons espoused by the Pardeys and others like them: reliable, easily replaceable in bad conditions when it will likely break (as opposed to winding cables inside a tiny compartment around a quadrant that is trying to slam back and forth), etc.
Over the four foot long tiller, that translates to 400 foot pounds of torque, so think of the driveshaft and transmission parts of an American V8, and that is the kind hardware strength and size you will need.
We ended up with a square stainless steel tube, 1 1/2" square with 3/16" walls, so the inside square ended up at 1 1/8", and then had the square rudder head that sticks through the cockpit floor (that the emergency tiller slips over) SLIGHTLY machined to 1 1/8" square on a vertical mill. (it only took a few thousands on each side) After that the square tube slipped over the top, and we basically welded the tiller arm pivot to the square tube, slapped on some tiller arms plates, and installed a set screw to keep it from moving or slipping off.
That said, I would have done something totally different, and would be more than willing to draw you up something that would be much better than our system (for free of course). It would involve splitting the ruddershaft/rudderstock and installing two keyed drive shaft couplers in the middle of the shaft under the cockpit sole so that the upper portion of the stock can be removed. That will allow you to drop your rudder without digging a 4 foot deep hole, and also allow you to use a standard cast bronze keyed tiller head, available at rigrite or any other retailer of old boat/big tiller stuff, and then you don't need to have custom built tiller heads. :P email me at: andrew.j.lea - gmail.com, and I'd love to talk more.
Where did you order the LED's encased in the rubber from?
ReplyDeleteDavid F.
http://www.domina-mea.com/